2026-02 – Compass Continued

The brass machine screws arrived this afternoon so once work was done I went down to the workshop to fit them. Although the required length is just 12mm I bought ones that were 20mm in length and cut them down to fit. The reason being that I’m more likely to use 20mm lengths and they come in packs of 20.

It didn’t take long to cut the machine screws to length, grind the ends so that a nut fits and then to fit them to the outer housing.

I still do not have a simple way to mount the LED in the bottom of the outer housing, so I just made up something that will do for now and if it proves to be deficient in any way then I can find a better way then.

I did take the time while the light was still in the sky to sand and put the fourth, and last, coat of varnish on the hatch runners. Once this is hard I shall put the hatch on, probably in a week or so since the temperature is still in the single digits and will be for at least the next week according to the forecast.

The mounting of the LED is not that difficult, it is the wires that are the problem.

So this is the way I’m going right now. This is the underside of the LED mount with the LED and the wires held to the wood with hot glue.

I have reassembled the compass, now to try out the lighting.

I have a variable power supply in my office which I set to 12V and connected the LED. This is the result with the office light on.

And with the office light off. Not at all bad.

Except that the inner housing has been put in backwards and the lubber line, which should at the front of the compass is at the back. So I will have to change that.

While I had the compass open again I took a photo of the LED mount. As you can see, it is very simple. Hopefully the huge blob of glue I put on the wires and wood will hold and stop them from being torn off.

Here is the compass the correct was around. You can see the word AFT on the outer ring at the bottom and the lubber line now opposite, where it should be.

So, the compass is done and now needs to be installed into the cockpit. But, since I get into and out of the boat on the starboard side, putting the compass in now would be right in the way, so I’ll put it aside somewhere safe and install it closer to the launch day.

Time for a cup of tea.

2026-02-03 – Compass Refurbishment

Shoal Waters was fitted with a ‘ fine brass binnacle compass’ (Sailing Just for Fun p113) and whilst it originally had a detachable domed top, complete with viewing window and side illumination, this has gone missing somewhere back in the mists of time. Still the compass survives but needs a little work.

Here is the compass disassembled. Originally, before being installed in Shoal Waters the compass gimballed in all axes, but Charles removed the fore and aft gimbal so that it just gimbals side to side.

I drilled out the 1/4″ holes in which the lugs of the compass inner housing located and press for four roller bearings, two in each side.

The lugs are quite sturdy and fit securely into the bearings.

The Bakelite bearing supports rest on two flat Bakelite pieces screwed to the outer housing and held in place by screws from the outside. These, being brass, had started to soften so I’ve ordered some more, but M5 bolts this time.

The holes in the Bakelite bearing supports were drilled out to 4.2mm and them tapped with a 5mm tap.

The bolts secure the supports inside the outer housing.

I used the M5 stainless bolts that I had available but these will be replaced with brass once they arrive.

The next task is to mount the red LED inside the housing which is not as easy as it sounds since the LED must not be too high or it will foul the inner housing as it gimbals.

This is where the compass is mount in the cockpit and you can see the small hole for the LED as it was originally mounted in the bridge deck rather than in the compass. I aim to change that and just have the wires go through the hole, probably through some sort of grommet that will also serve to stop water from going down the hole.

So. it is time to put the thinking cap on and devise a way to mount the LED.

Time for a cup of tea.

2026-02-02 – More Small Tasks

Just a few small tasks today, starting with applying the third coat of varnish to the hatch runners on Shoal Waters.

It is also time to apply some slippery gunk to the hatch itself. I made a jar of furniture wax a decade and a half ago consisting of beeswax, linseed oil and White Spirit for several projects I had back then. I made a lot more than I needed, but it has proved useful during the intervening years. I recently used it on two rope winding heads, on the teeth of the wooden gears.

Today I’ll use it on the htach.

This is the before photo, you can see that the wood is mostly untreated. It might have been treated with something originally, but years of sliding back and forth on the runners would have worn it off.

This is the after photo. I’ve applied two coats of the mixture. The white spirit acts like a solvent for the linseed oil and beeswax and penetrates the wood. The the spirit evaporates quite quickly and after that the oil slowly polymerises. The effect is to carry some of the beeswax into the wood leaving some on top of the wood.

The nice thing about this mix is that after a few days the surface of the wood is just covered with a thin layer of wax. If you get it on your hands or clothes, it is easily washed off.

The last task for today, I’m having a ‘rest’ day and not doing that much, is to cut the glass mat. I bought 2m of 1.27m wide 300g biaxial glass cloth and it needs to be cut in half.

Half of the mat covers the case side with plenty to spare, although I’ll probably need to cut it down to size a little more once it has been placed onto the pre-epoxied wood but before it is wetted out.

After this I folded both pieces up, put them into the bag it came in originally and took both the glass mat and the case side back into the workroom for the next stage.

Which will not be today !

Time for a cup of tea.

2026-02-01 – Port Centerplate Case Side, Again

It is February already and I need to get a move on. Still lots to do and time is starting to run out. The task for this wet and dreary day is to complete the construction of the port case side.

Unfortunately, the runner sprung slightly when I removed the cramps and I’ll have to do two things to rectify this. Firstly this gap needs to be cleaned out and filled and secondly, the runner will need to be trimmed on the bottom to compensate.

The first part is easy, a sharp chisel and some sandpaper and he job is done. The second part can wait until later when the pivot bolt hole is filled with epoxy.

Next task is to drill out the pivot bolt hole and to do this both case sides are clamped together and a 10mm drill drilled down through the completed starboard side drilling out the epoxy filled hole on the port side.

The next task is to make and fit the vertical support. Here I have already fitted the metal plate and marked the places where the screws will be put in from the inside.

The support was located using a 10mm drill bit through the support and the case side and then clamped in position so that the holes could be drilled through from the other side.

This is the inside and you can just see the tip of the 10mm drill bit in the pivot bolt hole.

Two of the holes were drilled and countersunk, then screws put in place to hold the support whilst the remaining four holes were drilled, countersunk and screws fitted. I use a vertical drill guide to make sure that the holes are drilled, well, vertically to the workpiece. I also drilled out the bolt hole to 13mm as was done before for the starboard side back on 1st January.

Once this was done, the mating sides of the support and case were lightly sanded, glue applied and the support screwed in place. The glue squeeze out was removed to reduce the work needed to clean up later.

Time for a cup of tea.

Having fixed the support in place it was time to move on to the diagonal brace.

I made a paper template from the first side and used that on the small angle jig.

Like this. This it was just a case of cut the end of the brace, make a template for the other end and then cut that to give me the brace with tapered ends.

Mark the position of the brace, drill holes through the side, clamp the brace in place and drill into the brace from the other side and chamfer the holes. Then glue it all together. Then I started shaping the ends to meet the runners and realised that I had made a critical error. The brace was the wrong way round !!

Fortunately, the glue had not started to set, so I hastily removed the screws, cleaned the clue (water soluble whilst still liquid) and put it on the other way around.

Here is the result and you can see where the brace was before. I’ll have to put epoxy in the screw holes to fill them up but I have to do that for the pivot bolt hole and the sprung section I referred to earlier. Once the side is installed into the boat and painted you probably will not notice the error. At least I hope so.

Now I definitely need a break.

Time for a cup of tea.

Before I took a break I brought both case sides up into the house to be in the warm since the next major task will be the epoxy, glass and graphite layers on the inside faces and the wood should be warm for that. Well, warmer than outside.

Then I took my tea break.

One I had consumed the tea I took the port side into the workroom, drilled out the errant screw holes to 12 mm, put squares of blue painter’s tape on both sides of each hole, making sure that the tape was pressed down firmly, then cut the tape on the top side to reveal the holes. The sprung section had tape put on the underside. Into these holes I put epoxy thickened with low density filler mixed to the consistency of double cream. I want it to flow into all the holes and fill them up without me having to press the epoxy in with a putty knife.

This is the sprung section.

And these are the screw holes. The blue bag you can see in the photo is a piping bag that I bought when I rebuilt Naiad. Well, I bought a roll of 100 catering piping bags and they are great for this sort of work and for putting down epoxy fillets with a stiffer epoxy mix. I used the slow hardener for this job so that the epoxy has time to seep into the wood fibers before curing to make sure that the hole is made completely watertight. A bit of an overkill, really, since this is the side that is going to be glassed but doing this gets to be a bit of a habit once you have done it a dozen times or more. Any hole that I make in a wooden hull, for example, is drilled out over size, filled with thickened epoxy and the correct sized hole drilled into the epoxy.

Before calling it a day I sanded the hatch runners on Shoal Waters and applied a second coat of varnish. It is currently 8º C and is forecast to be 6º to 7º between now and this time tomorrow, so the varnish should dry well in that time. Wednesday and Thursday are forecast to be a similar temperature, so I should be able to get another two coats on to complete that task. Then I’ll have to wait a few days for the varnish to harden completely before putting the hatch on.

The hatch is by the Rayburn until it is needed having had four coats of varnish all round. The day before I put it back on to the boat I need to grease the parts of the hatch that touch the runners so that it slides easily.

As I went out to the boat to apply the varnish, I noticed that I had left the cabin light on from this time last night. That means it has been on for 24 hours. The battery is an old one and doesn’t hold charge well any more, but the light was still on. Mind you, during the day I expect that the majority of the charge to the light came from the solar panels.

That, I think is it for the day.

Time for a cup of tea.

2026-01-31 – Completing the Case Side Removal

Although completing the removal of the port side of the centerplate case is a major milestone, the remaining tasks to do this are small. I did not need to remove the curved section of wood on the starboard side of the mast step as the already exposed inner veneer of the original plywood is quite firm, so I put a new blade in the multi-tool and set to.

An end-on view of the completed removal.

And a more informative view from showing the side.

Here is the short template I made yesterday in place showing the fit. Looks quite good from this angle.

But not so good from this. The gap is due to the top most runner on this side being lower than the one on the other side. However, this is not a big deal, I shall cut out a piece of marine plywood that will fit into the gap and glue it to the case side. That’s the next task, after I have had a break.

Time for a cup of tea.

To cut a correctly sized piece of plywood I first attached a gash piece of hardboard with hot glue so that the lower edge rested on the runner.

I found an offcut of marine plywood that is just too big.

Cut the required bevel on the end…

…and cut to size after running a pencil along the bottom edge of the hardboard. This is quite small and I wonder if it might be better just to fill in the gap once the side has been installed. The gap might just be a different size after the installation, so I’ll put this aside until after the centerplate case sides have been put in place.

Before I could do that I had to complete both ends of the space in which the new side will be installed. There were a few adjustments to be made since I left the ends too long deliberately, so that I could trim them back to fit the side.

This involved cleaning up the forward end of the slot as a fair bit of glue and original plywood remained at the bottom of the slot forming a lump that prevented the new side from fitting down into the slot correctly. There still remains some glue to be removed but the big lump had to go first.

The result, even without the complete cleaned out slot is pretty good.

The fit is snug to the side of the slot and I could probably get away with leaving the hard glue in place, but it comes out easily enough as it is very brittle and I’d rather get it out than leave it in and have it cause problems later on.

Here is the side from the cockpit and you can see the inner laminate fitting snugly into the aft block.

Time for a cup of tea.

The next task in the list it to make the new bottom runner for the port side. This was fairly straightforward, I had a piece of Sapele cut roughly to size and this just required cutting to a bit longer than required, the ends trimmed to match the old runner still left on the keel and then checked for fit. It needed to be reduced in height about 1mm and the upper corner that meets the side was chamfered.

Then the new side was put in place and the runner bent under to fit the curve and a pencil mark put on the runner and the side so that I can locate the correct position for the next part which is to drill holes, then glue and screw the runner to the case side.

The weather has been reasonably warm and by early afternoon the humidity had dropped, so I scraped and sanded the hatch runners and applied a coat of varnish. If the weather holds I should be able to get another coat on tomorrow afternoon.

Time for a cup of tea.

The last outside task of the day was to glue and screw the runner to the case side.

The screw holes that will hold the runner to the keel were drilled first and then the holes through the case side and into the runner. The aft end needed some persuasion to bend around the curve, hence all the gramps. Finally, the case side was brought into the house and leant up against the Rayburn to get warm.

Finally another coat of varnish was put on the hatch.

Time for a cup of tea.

2026-01-30 – Second Major Issue

The aim of the next few days and the weekend is to complete the build of the port side of the centerplate case and, if time allows, cut the aft block below the soft section.

The remaining part of the case side is the forward end and this needs to match the case side that has already been built.

I cut a matching end out of a scrap of plywood so that I can offer this up to the slot and block in the hull and make sure that it fits.

The it was a case of cut and chisel off, rinse and repeat.

However, when I reached the forward part of the section to be removed I found that the plywood was still quite soft and fibrous, or the middle veneer was. The outer veneers remained hard.

So I cut some more off until I reached plywood whose middle veneer was not soft. However, the problem, the second major issue, is that the plywood under the mast step part is soft and that means that the curved section of the step will need to be removed to see how far that soft plywood extends.

The curved section, seen here in Naiad, is not a single piece on top of the forward block, but two curved pieces screwed and probably glued to the sides of the block, so the removal should just be a matter of getting the brass screws out and cracking the joint along the glue line.

Should be. It remains to be seen if this is really the case.

The problem will be if the compression post is fixed to the mast step with screws. There is a stop block aft of the post to stop it from being pulled aft by the centerplate uphaul and I expect that this will need to be removed and it looks like the screws holding it in place may go into the curved pieces.

Once that is done then I’ll be able to take a closer look at how the compression post is fixed. The forepeak light is not installed yet so this will mean using a head torch to illuminate the area. It is also quite cramped up there, so working in that area will be restricted to short times so as to avoid cramps.

Time for a cup of tea.

Both the stop block and the port curved piece came off fairly easily. The brass screws in the top piece snapped off as did the ones in the curved piece but that also had four stainless screws that had to be unscrewed first. I took a look at the starboard side and that has the same four stainless screws. I presume that one of the previous owners noticed that the brass screws had disintegrated and added the new ones.

Three of the brass screw stayed in the centre block with just the heads snapping off on removal.

The brass screws in the stop block were punched out a little with a drift and then pulled out with pliers.

I needed to use a thinner drift for the screws in the curved piece, but they all came out without problems.

After that I carefully cut back the original plywood until I found a good inner veneer.

Given how easily the curved piece came off on the port side, I think I shall do the same for the starboard side and check the plywood under that. In both cases any gap between the new case sides and the original plywood will be filled in with marine plywood although I think I shall soak the edges of the original plywood with Clear Penetrating Epoxy Sealer, just to be on the safe side.

I will sand down the removed pieces, fill in the holes and drill new ones for the new screws as they will need to be in different locations so as not to foul the bits of the brass screws that remain in the block. I’ll probably just use thickened epoxy to fill the old screw holes rather than drill out the holes and plug them. It will not look as good but that part is rarely seen, so it will not matter.

That was it for the outside work for today, inside I turned the hatch over, which has been coated with four coats of varnish on the top and sides, sanded and varnished the bottoms of the sides. To prevent the new top surface from being marked I put a towel under the baking sheet which also serves to stop the hatch from rocking as I varnish.

All in all, a good day’s work and not so much of a major issue after all.

Time for a cup of tea.

2026-01-28 – Continuing Small Tasks

The weather has been just a tad cold this last week and I have been hard pressed to spend more than a few minutes outside before needing to warm fingers up again. I have concentrated on getting a few small, but necessary, tasks worked on, things that take less time than my fingers to get too cold.

The companionway hatch needs to be finished off. Firstly, the almost correctly sized machine screws arrived and I was able to trim these to the correct length. Unfortunately, these all ended up being slightly different sizes due to the irregularities in the slot. This is only a problem when the hatches is removed as the screws need to be labelled to make sure that they go back in the right place.

Which is immediately!

So, four machine screws carefully labelled.

The hatch was taken off the boat, sanded with 80 grit, then 120 grit sandpaper, using a paint scraper when necessary and then taken inside along with the can of varnish, warmed up by the Rayburn for a while, before being supported on a milk crate in the workroom to be varnished.

The top and sides were given a coat of varnish and the result is quite good.

I’ll put on three or four coats, lightly sanding between the coats before turning it over and putting three or four coats of varnish to the underside of the sides. One side is almost devoid of varnish and I may apply a couple more coats to this area. Once done I shall leave in in the workroom until I need the space to epoxy the centerplate case sides when I will take it down to the workshop and suspend it by the padlock staple from the rafters well out of the way.

The longer bronze screws for the port coachroof cleat also arrived and these were also trimmed to length and screwed in place.

The original screws protruded slightly from the backing pad but the replacements were trimmed so that they do not.

This is the pad before the update and you can just see the tips of the stainless screws protruding from the backing pad and whilst these are not in an easily accessible place, if you were to put your had up there you would risk getting you hand scratch as the points were quite sharp. The long black screw you can see in the photo was one of the temporary screws holding the solar panel in place. These have been removed and replaced with bolts, washers and self-locking nuts.

Whilst cleaning out some of the mess in the part of the keel slot that is on the long support I noticed that one of the screws through the original bottom runner that has been cut off extends out of the side of the slot. You can see the yellow brass top of the screw where it has been cut off and the threaded end of the screw in the side of the slot. This needs to be removed. There is another one on the other side of the slot a bit further aft which will also need to be removed.

The removal might be a bit tricky since I need to make sure that the side of the slot is not damaged in the process and I think that the best solution will be to cut off the part of the screw that protrudes through the slot sides.

I have a plastic handle device that holds a hacksaw blade that can be used in situations like this. One of the protruding screws cut off without problem but the other did not. Instead, as I pushed down with the saw to cut the screw, it started coming out of the hole downwards. After a few strokes I was able to pull it out completely with my fingers.

The best part is that I did not damage the side of the slot.

But, I have to fill the hole before I assemble that side of the centerplate case.

After I had finished work and whilst there was still a bit of daylight, I took a chisel and then 40 grit sandpaper to the top of the keel which is still looking a bit rough.

The easily removed pieces of the top runner have been removed and I’ve given it a rough sand with the 40 grit paper to remove any loose bits. I’ll dig out my belt sander and run that over the top to try and remove the stubborn pieces of glue and old runner. This top edge and the inside of the slot need to be free of old glue and wood so that the new case sides and runner can be bonded together securely.

I still have the forward section of the case to remove and also the aft block to deal with, but I am getting close to the point where I can finish the port case side at which point I can get on with the epoxy work for the inside of the case.

Time for a cup of tea.

2026-01-25 – Freezing Fingers Day

It is very cold outside today, not temperature-wise, although that is just 6º C, it is the humidity and the breeze. My fingers last just about half and hour before I have to retreat to the house to warm up, so just little things today, nothing major.

First up is the backing pad for the port side cleat. The screws I have are too short so I need to get some longer ones but I’ll leave these in for now.

Next up is to replace the port bullseye as it is somewhat worn. I have two left over from Naiad, so it is an easy decision to make the replacement. I was just going to remove the brass screws and put in bronze replacements, but decided against this when I saw the state of the bullseye. The one on the port side has very little stress as it is simply there to guide the furling lines, however, the screws need to be replaced. I also note that the inner Lignum Vitae ring is quite worn due to the small diameter of the furling lines running through it.

I managed to get three of the screws out, two unscrewed with a screwdriver and the other two had to be drilled out, the fourth screw coming out when I removed the block from below. The old holes will be filled in the next time I mix up some epoxy, the area cleaned, sanded and painted and the new bullseye will be fitted about half an inch back from the original site. This is because the two front screws screw into the end grain of the plywood of the sloped section of the coachroof which had two problems. The first is that this could allow water ingress into the edges of the plywood and the second is that this is not strong holding.

On the inside of the cabin there is a small shaped block that allows the two aft screws to screw into more than just the thickness of the coachroof, however it is to small and thin and has some water damage as evidenced by the darkened wood.

This is where the removed block is sited and it does look like there may be some water damage to the plywood from the front, right screw as you can see from the darkened area.

Still, on this side the stress on the bullseye is not great but moving the bullseye and block aft will allow a larger block to be used and for all four screws to be screwed into this thicker and stronger block.

This is the block on the starboard side of the cabin and here the story is a little different. The strain on the bullseye above this block is upward and aft as the topping lift runs through it. The screws have partially disintegrated as you can see from the left screw point here, it is covered in verdigris and I expect that when it is removed, these screws will be mainly copper. This block will be replaced, moved aft as for the port side and the screws replaced with bronze.

I won’t know if the bullseye this side needs to be replaced until I take it off and inspect it, which will be as soon as my hands warm up !

Time for a cup of tea.

Having warmed my fingers up and drunk my tea, I went back to Shoal Waters and took a look at the starboard bullseye.

You can see that the brass screws have been replaced with stainless indicating that the brass ones were too far gone and possibly even let the bullseye fly loose whilst in use due to the upward tension.

The bullseye itself looks to be in fairly good condition as the line running through it is a lot larger than the furling lines through the other one, but I think I’ll replace it as the topping lift is, as just mentioned, not a thin line and this is one of the smaller internal diameter bullseyes whereas the ones I have spare are larger.

Removing the screws and bullseye shows a fair amount of sealant under the fitting and the plywood looks to be in fair condition.

I took that block out from inside and here are the blocks, old and new bullseyes.

You will notice that not only is the starboard block wet and much darker than the one from the port side, but is is also split through the screw hole. So whether or not the bullseye needed to be replaced, the block underneath certainly needs to be replaced as it is pretty useless as is.

I’m hoping that the plywood of the coachroof in this area is still sound, I will have to take a closer look from inside at a later date. From the outside the plywood looked sound on both sides, but I’ve not checked the inside yet.

Thinking about the load on the starboard bullseye, I will probably make the new block substantially wider than the original to spread the load across more of the coachroof. There is an argument that suggests that the entire joint should be strengthened from one side to the other as I did in Naiad, but that would mean laminating a new beam in situ. I have the wood, epoxy and skills to do this but it is quite a lot of work that I don’t really need to do at the moment. Wider blocks should do the trick, so I think I’ll put this on the wish list for another off-season.

Conveniently, the angle on the forward side of the blocks is 45º, which means that this can be cut on the table saw. However, the coachroof is also curved.

So armed with the appropriate tools I measured the curve using a piece of cardboard for a template. From this template I cut a second template that mimics the coachroof, to use for shaping the blocks.

However, the curve is too slight to be able to cut accurately, so I’ll do this a slightly more messy way that will give an exact result. That is to cover the top side of the block with thickened epoxy with cling film on top of that and press the whole thing into place and keep it there with a prop from below. Once the epoxy has cured the block is taken down, the cling film removed and any squeeze out trimmed off.

The problem is that it is currently too cold for epoxy, so this will have to wait until either the weather warms up or I warm up the inside of the cabin with the new heater. Guess which one I’ll be doing!

But not today.

I did take the time to cut two pieces of Baltic Birch plywood that will be used for the blocks and round off what will be the visible edges. So as soon as the temperature allows, I’ll get the epoxy filler applied.

That’s all for today.

Time for a cup of tea.

2026-01-24 – Continuing the Case Side Removal

The weather continues to be reasonable for the time of the year, the temperature is currently 8º C, there is only a little wind and for a change the sun is shining. The main task of the day is to complete the removal of the old centerplate case side, hopefully this will not be an arduous task, but we shall see.

The first part of this task is to remove the screws from the outer runner. These are fairly easily found since they are set quite deep and have some sort of glue plug over the head. The procedure is to locate where the plug is, cut into the wood either side and inboard and then lever out the wood with a screwdriver. Thie wood tends to break at the screw head as shown here and thereafter it is just a case of clean out the slot and unscrew.

I bought some longer multi-tool blades to try and make the removal quicker and these are around 20 mm longer that the cheap ones I bought, which are perfectly good, just not long enough making the job a three cut process. With these longer blades that should be just a one cut processes.

With the stainless steel screws removed and using the longer blades, it did not take all that long to cut under the runners and remove the offcut.

There were some old brass screws holding the runner runner to the keel but these were sufficiently soft that the blade cut through them.

This is the result after cleaning up the mess. I still have the section around the forward case block to work on, and to remove the parts of the runner still glued to the keel as these were cut just above the glue line in order to avoid cutting into the keel at any point.

I decided to take a break at this point and checked out the wooden pad I made last night and painted first thing this morning. It should be good for a second coat later on today.

This pad will sit under the bronze cleat on the port side of the coachroof as the solar panel now sits quite close and this cleat needs to be a little higher than before.

It isn’t the solar panel, per se, but the plastic block that houses the connections. I will also need to make three risers just aft of the two through deck fittings and also in front of the cleat so that the furling lines do not chafe the fittings when in use. If I have enough copper plate then I shall cover the top of these risers so that they are also protected from chafe.

Time for a cup of tea.

I have to say that I gave up on the case side removal for the moment as my knees are complaining. I should have bought a pair of knee pads years ago but never did and now my knees are suggesting that now would be a good time.

So, instead I worked on the main hatch which just needs to be fitted before it is ready for sanding and varnishing, which can be done in the workshop and will not get in the way of work in the boat.

This task involved drilling four holes in the sides of the hatch, threading them, inserting the machine screws that will retain the hatch and testing for the fit. Sounds easy but the process took over two hours to complete.

The machine screws that were in the hatch before are Imperial, not metric and I do not have a tap of the correct size. Nor do I have the metric equivalent tap of M6, so I opted for M5 screws for which I do have the tap. Unfortunately, I do not have the correctly. sized machine screws. So I used M5 x 50mm to get the fit correct which will then tell me the correct length of screw to buy.

I put the hatch in place and marked the top and bottom of the slot in the runners at each of the four corners of the hatch. I used a thin line around the side of the hatch to transfer the centre of the marks from the inside to the outside, one side of the hatch at a time. The first hole I drilled I did from the outside and it was far too high. After this I drilled the hole again but this time from the inside and the screw came out in exactly the correct position. Having drilled the hole I tapped it and put in the over-long bolt. The hatch was put in place and the bolt carefully screwed in whilst I squinted down the slot.

This was repeated for the other three holes and each one, drilled from the outside, came out correctly. I put the hatch in place and carefully screwed in all the bolts until I found the place where the first one started to bind in the slot. I measured the length of the bolt sticking out of the hatch and set the other three to the same length and checked that the hatch not only slid freely but did not come off.

Having measured the length of the bolt and done some simple maths I need to buy M5 x 27.5mm machine screws….which do not exist.. That means I’ll buy 30mm instead and grind them down to the correct length.

Bolts protruding one side…

And the other side.

Time for a cup of tea.

Since there was still some useable light, even though the sun was low in the sky, I decided to get another task off the list, if possible.

The solar panel is now properly fixed and the deck glands are also done. Not only is this another task off the list but I don’t need to charge the battery with the battery charger any more. Even though the solar panel is under the perspex roof, it generates enough power to charge the battery even in the Winter light levels. Mind you, this is an old battery and well past its useful life, so it will be replaced with a new one once we get closer to the launch date.

Time for a cup of tea.

2026-01-23 – First Major Issue

Things have been progressing well on Shoal Waters since we bought her last June and the repairs have been going well with no major problems.

That ended today.

The rotary tool saw blades arrived late yesterday so first thing this morning I went down to the boat and used the smallest to cut into the area of the aft centerplate case block that could not be reached any other way without dismantling the cockpit.

This is what it looks like when attached to the extension and cordless drill.

And it worked quite well, although you do need to hold the tool very carefully since it can easily run away from the workpiece despite its small size.

Having cut “along the dotted line” so to speak, it did not take long to remove the old plywood and that is when I noticed the problem.

Here. This bit is soft and has no structural integrity. There is no way that I can install the new case sides with the aft block in this state and this has to be repaired or replaced.

The options are limited.

  1. Cut out the soft section leaving as much of the good wood as possible and fill in any gaps with a graving pieces.
  2. Cut off the top of block below the soft part and make a new top section.
  3. Remove the entire block and make a new one.

Option 1 is going to be difficult since the soft parts are not contiguous and that means cutting out several sections and replacing them.

Option 2 seems to be the best option if I can find out where the soft section ends.

Option 3 is the most drastic but has the issue that getting out the section that is recessed into the keel is not going to be at all easy.

I’ll leave this part for the moment and continue on with removing the remainder of the case side whilst I ponder on this some more. Hopefully the forward block will not suffer then same affliction.

My immediate thought is to make a template of the entire block above the keel and then cut the block just below where I know the soft section ends. If that is the end of the soft area then I can make a new top section and fit it to the old base part. If the soft area extends down further then I’ll cut off more and more until I reach good wood and make a new top section. If the soft wood extends below the level of the top of the keel then the whole thing will need to be removed and a new block made and fitted.

I really hope that the latter is not the case since it is possibly as much as a month of work to carry out. Still, if it needs to be done, then it needs to be done.

During my lunch break I took a sharpish pokey thing into Shoal Waters and prodded the aft block.

The soft section that I can easily detect is quite high up on the block, so it may be that the repair will not be quite so drastic as I first thought. Still, I’ll find out more once the top of the block has been removed.

Now, some people might say that the wood sounds soft all the way down as it is giving a muffled return all the way down. To which I would say that you need to remember that the top of the block is unsupported and that allows the whole thing to vibrate like a tuning fork and for that reason I would expect the return to be a bit muffled. However, the soft section certainly gives a much clearer soft return.

I have also been chopping away at the bottom of the block with a chisel and that showed that the bottom of the block is still quite solid.

So, the way forward from here is to cut off the top section below where the soft returns are being heard and see what the wood looks like inside.

Time for a cup of tea.